dear experts ,
After a hard #workto reduce noise for certify our equipment directive CISPR 16-2-3 class B with LNE , i had basically tow problem :
1- harmonics 50 MHz oscillator for Ethernet 10/100M design in mother boar. that is not the point of this post.
2- noise in power supply of our mother board we use a SEPIC DC DC converter 24w large input 9-30v and fixe output 12v@2A. for conducted emissions it was goodbut for radiation emissions it was very Noisy so I started dig into the issue and what is the source of this noise, hot loop as small as possible , ground MOSFET as close as possible to gnd output capacitor , change référence of components with better intrinsic characteristics change PCB placement and layers .... keeping in the mind the price of those changes and the most important thing the right functioning of the board
So now i can say i was very successful reduce noisebut when i measured temperature of components, the surprise :
-Before modification at max load 2A :
- Coupled inductor : 49°
- Diode : 55°
-Mofet : 45°
After modification :
- Coupled inductor : 64°
- Diode : 68°
- Mosfet :77°
Note : i take those measurements with my old multimeter and K probe thermometer
So maybe i know whyi use a 50R for gate Mosfet so i think i should find another method like use 4 layers PCB.
TO YOUR KEYBOARD for any help
Hi, thanks for your reply and information.
i dont know how i can do professional pcb and control current return path (if iam an professional designer pcb i dont think i post this TOPIC). I tried with one version to delete gnd plane in top layer and use only piste and via gnd but (2layer and 4 layer it was my first change) i didnt see a big diffrence so i dont know how i can do better, that why i ask help in forum ?You pour polygon all PCB surface, that mean, you don't care or control current loop. We will not sure how current flow, where current run. Pour all PCB is not for professional designer.
how i can know if they have same path or not ?Confirm that: dc current run through the shortest resistance path, but ac current through the shortest impedance path. This means dc & ac current in poured PCB is not same path. TROUBLE !!!!
no.Do you know microven-oven principle ?
oky, if u mean switch frequency its around 333khz so Wavelength is 900m so 90 m ?You poured double PCB made a C, the far connection vias connect two GND mad L. When excitation signal appear, the L&C will ringing with very high frequency. That why, PCB layout has rule: place vias near cornner of PCB, or beside the high speed path. The space ~= 1/10 length of that frequency. You didn't do this on PCB.
i think that what i did , i have only 2 piste on the bottom , all other piste are in TOPTry to place all power trace, current loop in same layer.
i didnt do test with this version , but with the origial pcb version it was good. but i will do with my final version to see if i didnt worstit.I still suspect you may have conducted issues emissions issues and depending on the loop area of your wiring your problem will vary.
yes but when u say "all the damping" if talk about R9,C17 (DIODE) and R10, C18 are not connected (NC) , for me i have only gate resistor 50R.By adding all the damping you've just added loads of loss hence the heat. Theres a few things i'd look at if i were you
1-about input filter i have in mother borad PI filter but i use only inductor 150uH1. Add an input filter as the switching currents will be in the power lines, the size of the loop of the power wires will make them antenna, if you can't add a filter then make them a twisted pair or ensure the are in close proximity (touching) and hope for the best. Bigger the loop the worst it will be for radiated emissions. You haven't shared the details for the input current ripple of your design but you only need uA's of switching ripple to give you all those harmonics.
oky i will see but2. Similar to the input. Your output inductor is far too physically small and is likely not an inductor at all with a output current of 2A as its saturated, The Datasheet suggest its max Current is 1.2A but for it to be 1uH the current is more like 200mA. You need to replace it with a propper power inductor (which is screened) with at least a 2.5A rating. Currently its doing next to nothing for you. You have 2 loads connected and as the wires aren't twisted you have two loop areas to radiate unless you remove the secondary switching currents off the line.
We talked much about the in your previous thread.i didnt see a big diffrence
No i didnt , but as i said i am not professional pcb design yet, so maybe i understand but i dont know how i can apply it my pcb design .....Sadly you ignored all this in your actual PCB layout (At least it seems so)
Taihung is very right with all he is writing.
yes its not clear yet !Hi
From your side it maybe not clear all "trick" to do with design.
ok i can understand.I really don't like using vias in power application and "auto stiching vias feature"
yes but as i share the result its oky with 50R so i want use only 5R and try to reduice nois noise with other method as i said 4 layer or change current path but the pcb design its now verry better then the first one but i should test the contucted emission if its still oky ........Your current paths is still not perfect yet.
i dont know how i can do it and i should be sure it will be decrease my noise to do it ....You did not separate power GND vs signal GND. The GND can complete on TOP,
i use or i want use only 2 layer pcb so plane GND is in the bottom for me.But i want learn if its possible design without GND in the bottom and i will be verry happywhy need through vias to bottom ?
yes by test i change and i test a lot of value but no changing in radited noise but in conducted they are usefulInput filter or ouput filter maybe not help you so much, sometime made more noise to circuit.
oky i can and i sharte it schematic what i cant share is the vlaue of PI regulator R7,C12,C13 and i want learn and do all change by myself , in this case i can ask an comapnay to do the job for me.If you don't mind, share project schematic & pcb to me, without company info, no logo. I will help you correct the rest in few days. Only hope you can share test result to forum.
You can see my reply #14 , and if u think i have school lever its not a probelem for me. reply me about post #12 u said Taihung is very right with all he is writing. and me i said tank you Taihung for all ur response but iam not agree with u in this point and i say why. This a method to change idea and leanA forum can not replace school or your own learning, like going through tutorials, papers, videos.
Also you can´t expect that others do your job. (again and again)
i never ask u to reply and spent time , if i post my question is about to change informations and learn each otherI won´t spent the time to repeat the same as in the other thread.
No i will be a senior in some years and i dont want the easy method i am here to learn , if do something wrong or this forum doest like what i do i can change it and never post my question here , no problemMaybe consider to hire a senior designer to assist you.
Klaus
for change frequency i will see what i can do ! thanks for all those informationsHi
You can add me taihung7z@gmail.com. I am not so friendly with EasyEDA. I often using KiCad. But, I tried before.
oky , its very easy and good free software , i cant add u should create an account with ur adress then i can add u and share project .... let me know when u did it.
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