skn96
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Thanks for your response Akanimo
The reason I was reluctant to add scrubber across the 16 gage wire was I though it will steal some of the current that is sensed by CS1 and may affect precision of current control at the fundamental frequency which is 100kHz. . If I want the snubber to damp 10mHz ringing it will have some minor impact on the 100kHz current also. But I don't know if it is ok or not. Do you any experience with that?. It is my firs kW watt experience with full bridge topology and wasn't sure adding snubber in parallel with current sensing path how will impact the current control performance. By the way in the formula you presented by leakage inductance do you mean the resonance inductance which is in the order of 20uH or the parasitic inductance of input traces and 20cm wire which is in the order of nano hanries?
The MUR1540's are snappy diodes, and will need snubbing, all PSFB converters need real diode snubbing at load... if you are going to go to 2400W even for 2 sec, better to use the best diodes you can get, this will reduce the snubber power required.
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