T
Thanks, if its not a differential measurement, then it must be common mode?As far as I'm aware of, there's no differential measurement intended.
To give a sweeping answer: Understanding why the switcher will spread not negligible conducted noise although it's equipped with a seemingly ideal filter is the very start of real EMC engineering...However, Another thing is that surely the conducted emissions graph on page 23 of RDR-506 looks wrong? I mean, if you look at the schematic of the buck converter on page 5 of RDR-506, it has a really heavy PI filter consisting of a 1mH inductor and a 4.7uF capacitor either side of it………for a buck converter of just 1.44W rating, that is an extremely heavy filter….how can all the Megahertz frequencies on page 23 of the RDR-506 document be there?
Thanks, i believe you are speaking of the parasitics of the filter?......and the MHz frequencies are simply going through the interwinding capacitance of the inductor?To give a sweeping answer: Understanding why the switcher will spread not negligible conducted noise although it's equipped with a seemingly ideal filter is the very start of real EMC engineering...
We use cookies and similar technologies for the following purposes:
Do you accept cookies and these technologies?
We use cookies and similar technologies for the following purposes:
Do you accept cookies and these technologies?